Well I have good news and bad news. First, the good news. The Cobra made 56 rwtq more than it did with the old engine even though Steve stopped the pull at 4000 rpms. He stopped it because the AFR went below 10:1 as soon as he went full throttle. So even with a very rich and short pull it still made 56 more tq. The biginning of the bad news is that the chip I have is Autologic and can no longer be programmed. So I have to buy a new chip so Steve can tune the car. Since I don't have the money to buy it now I'm going to have to wait for the tune.
The rest of the bad news is that Steve also says that the vibration is a balance issue and not the tune or a misfire. He hook up a scan tools and monitored everything and says the engine is running great. So I'll be calling CHP on Monday and see how they want to procede but the engine is going to have to come back out and torn back down.
Guy also had issues but I'll let him update them on his thread. However, Steve also made a pull on his and cut it off early as well. I think he cut it off at around 4800 when the supercharger belt slipped but by 4000 he was already making 10psi of boost. With our short runs I think he made 2 rwhp more than me and I made 22 rwtq than him.
Last edited by 94cobra69ss396 : 01-05-2013 at 08:53 PM.
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